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Unusual Failures in Hydrogen Production

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Unusual Failures in Hydrogen Production Sheldon W. Dean Dean Corrosion Technology, Inc. Allentown, PA May 17,2005 Hydrogen is New Opportunity Ideal fuel for fuel cells. – PowerPoint PPT presentation

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Title: Unusual Failures in Hydrogen Production


1
Unusual Failures in Hydrogen Production
  • Sheldon W. Dean
  • Dean Corrosion Technology, Inc.
  • Allentown, PA
  • May 17,2005

2
Hydrogen is New Opportunity
  • Ideal fuel for fuel cells.
  • Exhaust only water.
  • Energy conversion is efficient.
  • Fuel for engines.
  • No hydrocarbons or CO in exhaust.
  • NOX can be minimized.
  • Other uses
  • - Removal of S, N, etc. from fuel.

3
Steam-Hydrocarbon Reforming
  • Largest source of hydrogen today.
  • Methane (natural gas) feed.
  • Higher hydrocarbons can be used.
  • High temperature-catalytic process.
  • Used for more than 50 years.

4
Steam-Hydrocarbon Reforming
  • Reforming reaction
  • CH4 2H2O ? CO2 4H2
  • Typical conditions 1650ºF (900 ºC) 600psi with
    excess H2O.
  • If higher hydrocarbons are present
  • CxHy (2X - ½Y)H2 ? XCH4
  • This step is run before reforming.

5
Typical Reforming Process
  • Pre-reforming (hydrogenation)
  • Steam introduction
  • Reform over catalyst
  • High temperature shift reactor (HTS)
  • Low temperature shift reactor (LTS)
  • Cooling and water condensation

6
Materials Problems Involving Corrosion
  • HTS inlet piping Cracks in bypass
  • (KOH SCC ).
  • LTS exit piping Cracks in mixing tee
    (corrosion fatigue).

7
HTS Inlet Bypass Cracking
  • BACKGROUND
  • Large steam hydrocarbon reformer.
  • Feed CH4 and some higher HCs.
  • Potassium promoted reforming catalyst.
  • Start-ups run with nitrogen then steam.
  • HC feed added when plant temp. OK.

8
Background Continued
  • HTS designed with bypass for start-up
    acceleration.
  • HTS piping 1¼ Cr, ½ Mo steel.
  • Bypass 304 SS because of possible condensation
    during operation (carbonic acid corrosion
    concern).
  • Operating temp 850 ºF (455 ºC).

9
HTS Cracking Incident
  • Many start-ups in first 6 months (gt10).
  • Then 2 months continuous operation.
  • HTS by-pass split open and tore off suddenly!
  • Shock wave and fire resulted.
  • Explosion heard 30 miles away.
  • Repairs required 3 months to finish.

10
Diagram of By-pass
To HTS
By-pass 304L
1¼Cr,1/2Mo
Location of cracks
11
Failure Analysis HTS By-pass
  • Many cracks found on interior of 304L.
  • Pipe interior has black oxide.
  • Cracks show white halos.
  • Samples of pipe with crack taken.
  • Metallographic sections examined.

12
Photo of Pipe Interior
13
Metallographic Section
14
Failure Analysis Continued
  • Cracked section broken open.
  • SEM examination of fracture surface.
  • Energy dispersive X-ray analyses of fracture
    surfaces.

15
Crack Fractograph
16
EDS Analysis
K
17
Results of Failure Analysis
  • Cracks are transgranular and branched.
  • Cracks are typical of caustic SCC.
  • No evidence of sodium present but potassium is
    widespread.
  • Residual stress in pipe from cold forming.

18
Conclusion
  • Pipe failure caused by KOH SCC.
  • Surprising because SCC usually causes leak
    before break in 304L Catastrophic SCC failures
    are rare!
  • Questions Where did KOH come from?
  • How did it survive in by-pass but did not crack
    1¼ Cr, ½ Mo steel pipe?

19
Investigation of Source of KOH
  • Transfer line refractory not source.
  • Waste heat boiler not source.
  • HTS catalyst not source.
  • Reforming catalyst is source
  • Potassium promoted catalyst.
  • Depletion of K found in catalyst.

20
Source of KOH
  • Potassium carbonate added to catalyst.
  • Carbonate decomposes in hot steam
  • K2CO3 H20 ? 2KOH CO2
  • KOH vaporizes during start-up when hot
  • 1788ºF (976ºC) V.P. 40 torr
  • KOH deposits on cool bypass.

21
Laboratory Study
  • Purpose to define when KOH SCC occurs.
  • Use ASTM G 129 Slow strain rate method (SSR).
  • Because water partial pressure fixed only one
    variable (temperature) available.

22
KOH Lab Study
  • Temperatures 370, 420, 550ºF (188, 216,
    288ºC).
  • 304L, 1¼Cr, ½Mo steel specimens.
  • KOH concentrations calculated for each
    temperature.
  • Head space had H2 added in some tests.
  • K2CO3 added in some tests to 90.

23
Results of Lab Study
  • 304L specimens did not fail until 50 psi H2 or
    CO added to head space.
  • 304L OK at 370ºF, failed at higher
    temperatures.
  • 1¼ Cr, ½ Mo steel failed at 370
    º,420 º but not at 550 ºF.
  • 90 K2CO3 caused no change.

24
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25
Recommendations
  • Redesign by-pass with free draining 1¼ Cr, ½
    Mo steel material.
  • Questions for further research
  • Why is hydrogen necessary for SCC ?
  • Is there an upper temp limit for 304L?
  • Are other alloys better for piping?

26
Mixing Tee Cracking
  • Background
  • Large hydrocarbon reforming plant.
  • Feed refinery off gas (mainly methane).
  • Condenser used as boiler water pre-heater.
  • By-pass used to prevent boiling in BWPH.

27
Mixing Tee Incident
  • Plant operated for about 3 years.
  • Leak noted in mixing tee at exit of BWPH.
  • Plant shut down and inspected internally.
  • Extensive cracking found in tee and down
    stream, also in expander.

28
Concentric Cone Heads
315F
220ºF
BOILER WATER PREHEATER
Location of cracks
Control Valve
Expander
By-pass Line
29
Failure Analysis
  • Most cracks associated with welds.
  • Metallography some cracks straight, others
    branched.
  • Some cracks showed beach marks.
  • Fracture surface quasi-cleavage.
  • EDS shows faint Cl and S on fracture surface.

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35
Investigation
  • Several older plants had similar cracks.
  • Found in hydrocarbon reformers (not natural gas
    feed plants).
  • Upgrade to 316L or Alloy 20 not successful.
  • Upgrade to 625 successful.

36
Laboratory Study
  • ASTM G 129 SSR tests.
  • Cyclic straining tests
  • 0.3 offset pre-strain,40.7 to 13.7ksi stress
    range.
  • 2000 cycles _at_ 1 Hz.
  • Potential control, Ag/AgCl ref. electrode.
  • 304L, 2205, 625 specimens.

37
Results 304L
  • No cracking with SSR tests.
  • No cracking with cyclic straining w/o
    electrochemical polarization.
  • Cracking gt200mV, 10ppm Cl-, 150ºC.
  • Cracking gt200mV, 1ppm Cl-, 1ppm NaCNS, 150ºC.

38
Results 625 2205
  • No cracking in cyclic straining tests up to
    600mV.
  • No cracking in SSR tests.

39
Conclusions
  • 304L shows synergistic cracking in water with
    Cl- and potential gt 200mV.
  • SCN- aggravates chloride cracking.
  • Both 625 and 2205 resist cracking.

40
Recommendations for Plant Design
  • Minimize thermal cycling of equipment.
  • Use resistant materials (2205 or 625) where
    thermal cycling occurs.
  • Avoid concentric cone heads on heat exchangers
    where condensation occurs.

41
Issues for Further Study
  • What are the effects of other impurities in hot
    water on corrosion fatigue?
  • What role does corrosion play in the cracking
    process?
  • What other alloys resist corrosion fatigue?
  • Can we predict cracking susceptibility?

42
THANK YOU!
  • Acknowledgement
  • Air Products and Chemicals, Inc.
  • Intercorr International Inc.
  • W. R. Watkins
  • K.L. Baumert
  • J. W. Slusser
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