Operation TCR - PowerPoint PPT Presentation

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Operation TCR

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A UPS supplying the PLCs for the demi water stations had tripped due to water infiltration ... seen when compensator in BB3 tripped. SPS stopped for 1h each ... – PowerPoint PPT presentation

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Title: Operation TCR


1
Operation TCR
2nd of July to 10th of September 2001 More than
20 major events Events grouped by equipment group
and zone affected
  • Niels.Schionnemann_at_Cern.ch

2
Electrical events
  • 19/08 1842 Electrical disturbance of 400 kV EDF
    due to storm, main PS magnet tripped. No
    electrical equipment switched off.
  • 1915 PS running again
  • 19/08 2108 Compensator 1 BE tripped due to
    storm. SPS and PS stopped.
  • 2121 PS running again
  • 2140 Meyrin filters fall out. PS still ok
  • 2214 Compensator in BE ok, SPS running
  • 2229 Meyrin filters ok
  • 20/08 0034 Compensator 1 BE tripped due to
    storm. PS and SPS stopped
  • 130 PS and SPS running again

Niels Schionneman ST/MO/TCR
3
Electrical events
  • 20/8 0648 Short circuit in transformer EHT3 BE
  • Transfo was idling but the short circuit caused
    an unbalance in the network and made the
    compensators trip.
  • Demi water off Prevessin and Meyrin
  • PS and SPS stopped
  • Electrical problem solved at 720
  • Cooling PS ok at 920
  • Cooling SPS ok at 1020

Niels Schionneman ST/MO/TCR
4
Electrical events
  • 29/8 1847 Explosion in 18kV breaker sub-station
    7
  • 7 18kV breakers in the PS loop trip
  • The 66kV supply for the transfo SEH1 tripped.
    Meyrin off tension
  • Auto transfer switched to EOS after 5 sec
  • The 18kV trips due to malfunction of protection
    equipment/selectivity problem
  • PS and SPS stopped for 24h

Niels Schionneman ST/MO/TCR
5
CV events concerning PS
  • 3/7 1420 Water leak alarm in PS
  • Demanded access but found no leak. Drains were
    blocked and condense water from air condition
    caused the water level to raise
  • 1533 PS running again
  • 4/7 2143 Cooling problem in 361
  • MCR can not switch on main magnet due to high
    temperature in 361
  • Ventilator in cooling tower not running on max
    speed
  • 2343 PS running again

Niels Schionneman ST/MO/TCR
6
CV events concerning PS
  • 15/7 901 PS demi water stopped
  • A UPS supplying the PLCs for the demi water
    stations had tripped due to water infiltration
  • UPS bypassed and PLCs and water stations started
  • 1125 PS running again
  • 19/8 243 and 719 Demi water station 359
    stopped. PS stopped
  • Station stopped twice due to heavy storms.
    Started station manually
  • 305 and 739 Cooling ok

Niels Schionneman ST/MO/TCR
7
CV events concerning PS
  • 20/8 1900 Demi water for TT2 stopped
  • No beam for SPS
  • No alarms received in TCR
  • Magnet in TT2 supplied from TOF line. To be
    changed
  • 2020 Cooling station in 378 started again
  • 23/8 2015 Demi water temperature too high in
    East area
  • Pumping station running on max
  • Primary water temperature at 25 degrees due to
    very warm weather.
  • Informing MCR. Situation unchanged all night

Niels Schionneman ST/MO/TCR
8
CV events concerning PS
  • 25/8 1510 Pump in cooling circuit for ISOLDE
    exploded
  • ISOLDE stopped
  • No fluid alarms in TCR, only electrical alarm
  • Isolated pump and started spare pump
  • 1540 Cooling ok

Niels Schionneman ST/MO/TCR
9
CV events concerning SPS
  • 6/7 1745 Temperature interlock on main magnet in
    BA3. SPS stopped
  • Supply valve closed on primary side of heat
    exchanger
  • 1938 SPS running again
  • 9/7 1145 Temperature interlock on septum magnet
    in BA6. SPS stopped
  • Pump stopped by faulty pressure sensor
  • 1230 SPS running again
  • 27/7 1025 BA6 cooling off. SPS stopped
  • CV working on PLC for BA6 cooling. A faulty
    Siemens module caused the station to stop
  • 1055 SPS running again

Niels Schionneman ST/MO/TCR
10
CV events concerning SPS
  • 2/8 1427 Demi water BA81 stopped due to water
    leak. No beam for North area
  • Access to machine given but leak is not found
  • Manages to start pumps and refill continuously
  • 1539 North area beam back on
  • 5/8 Compensator tripped due to missing cooling in
    BA3. SPS Stopped
  • No alarms in TCR
  • Cooling stopped due to problem with the PLC
  • 1940 SPS running again
  • 10/8 2040 Same problem as above
  • 2130 SPS running again

Niels Schionneman ST/MO/TCR
11
CV events concerning SPS
  • 27/8 420 Cooling for septum magnet BA2 stopped.
    SPS stopped
  • No alarms in the TCR. Pump restarted from TCR
  • 422 SPS running again

Niels Schionneman ST/MO/TCR
12
CV events concerning SPS
  • 2/9 431 3/9 456 Demi water BA3 stopped. No
    alarms in TCR
  • Problem seen when compensator in BB3 tripped
  • SPS stopped for 1h each time
  • Cooling stopped due to error in PLC
  • 3/9 2359 Demi water for CAV2RF1 BB3 stopped
  • SPS stopped for 3.5h
  • Cooling stopped due to electrical problem on pump
    for CAV2 circuit. Pumps started in forced mode.

Niels Schionneman ST/MO/TCR
13
Various events
  • 14/7-15/7 RTserver crashes several times
  • Different zones at Meyrin without supervision for
    various periods.
  • Fire brigade instructed to do rounds and keep a
    close eye on the synoptic.
  • 16/7 Bugs found and fixed by IN. Situation back
    to normal.
  • 27/8 355 Vacuum sector valve closed TS1 and TS2.
    SPS stopped.
  • 400 Valve in TS1 opened. OK for SPS
  • 410 Valve in TS2 closes
  • 412 Valve in TS2 opened. OK for SPS

Niels Schionneman ST/MO/TCR
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