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Barrel Harness Status

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... were used at Radiantech but...clear evidence of ESD damage seen ( photos) ... Simple cheap BER test system being made by Minglee (end May) ... – PowerPoint PPT presentation

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Title: Barrel Harness Status


1
Barrel Harness Status
  • Problems with DORIC4A.
  • Tolerances and fibre layout.
  • Harness status in Taiwan.
  • Harness testing at RAL.

2
DORIC4A problems
  • DORIC4As tested on wafer and only good die were
    given to Taiwan.
  • Yield of DORIC4As when mounted on doglegs was
    50. ESD precautions were used at Radiantech
    butclear evidence of ESD damage seen (? photos).

3
DORIC4A Solutions
  • Process changed to avoid sharp pointers and use
    automatic die bonding.
  • 122 DORIC4As now mounted on doglegs and all
    tested to work.
  • Dont want to use DORIC4As mounted on doglegs
    before procedure was changed because of worries
    about long term reliability.
  • Difficult to re-work doglegs because of cover.

4
Harness Lengths
  • Better definition of tolerances and which lengths
    are the critical ones to measure.
  • i/f PCB to PPB1 -0 20 mm
  • i/f PCB to MT connectors -0 20 mm
  • Position of MT splice /- 10mm or up to -50mm if
    splice needs to be redone.
  • Detailed harness engineering drawings showing
    fibre layout and check lengths (? figure).

5
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6
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7
Fibre Layout
  • Jigs produced in order to ensure correct fibre
    loops for fibres leaving doglegs before harness
    clip.
  • Photo shows prototype jig.

8
Schedule
  • Batch process so many steps well advanced
  • Opto-packages for 55 harnesses.
  • Doglegs assembled for 23 harnesses.
  • 4 Harness completed May 5th
  • 20 Harness completed May 13th
  • 36 Harness completed May 15th
  • 64 Harnesses (all B3) by May 31st
  • Complete all barrel harnesses by August 25th.
  • See schedule on web
  • http//www-pnp.physics.ox.ac.uk/weidberg/producti
    on/Barrel_Harness_Schedule.xls

9
Harness Testing at RAL
  • Complete system for bench testing barrel
    harnesses is working at RAL and was used to test
    the first two barrel harnesses. Software ok.
  • Current system requires temporary cables to be
    connected to PPB1.
  • Upgrade test system to use TPPs and TIs. The TPPs
    and TIs would then stay with the harness during
    subsequent assembly of harness to barrel.
  • Minimise number of connections made to PPB1.
  • TIs and TPPs should be available in 1 week.
  • System for testing harness on barrels still being
    developed.
  • Loop back PCBs (send TTC ? data links)
  • Simple cheap BER test system being made by
    Minglee (end May).
  • Allows for BER testing of 4 harnesses in parallel
    (could be done overnight).
  • Testing Harnesses on receipt of barrels at
    Oxford.
  • Simple loop back PCB tested and works.
  • Requires ROD software to use this (Peter
    Phillips).
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